Tuesday, April 2, 2013

A different kind of motor

With my 351W out of my garage, it was finally time to start thinking about reassembly...or at least getting the rest of the car ready for reassembly, which is obviously something quite different. I'm pretty sure it's a requirement of any worthwhile Mustang restoration that you "do the heater box" while the motor is at the machine shop. If not, it should be! My version started with liberating the heater box from its packing crate. I've moved house garage twice since the heater was put to bed, so it was fortunate that I packed it well.


The last time I saw my heater box was in early 2010, so I was actually a little bit shocked to find out how crusty it was. But then again it will be 45 years old in August. Unfortunately, I forgot to break down the unit....which meant all the metal parts missed out on my batch refurb/painting process. Oh well...


Started by removing everything from the heater case. Ford did not design the heater unit to come apart, so the tear down involved drilling out plenty of pop rivets. The blower housing was a bit rusty: especially in the places where it wasn't originally painted (like the whole car!).

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There were a few cracks in both halves of the case...but nothing a bit of superglue couldn't take care of.


The first major positive of this mini-project was the chance to once again fire up my favorite dewalt angle grinder and its knotted wire wheel. All the metal parts got a good going over before you could say "rust removal". Well not quite that fast, but you get the idea.


The flapper unit was a challenge too far for the wire wheel though, so I legged it over to Mostly Mustangs in Oakland and swapped a six-pack for twenty minutes fun in their blast cabinet. Lovely.


The cleaned up metal parts were wiped down and painted with primer, and then I laid down several coats of the same black paint I used on everything else.


I painted the exterior brackets and some of the other parts with my favorite Eastwood brake gray. This is an old BAMA trick that is designed to make sure everyone knows you took the entire unit apart...and it's use is most definitely not restricted to the heater box.


Initially I wasn't going to paint the heater box, but it didn't look right next to the cleaned up parts....so I hit it with two coats of black fusion-for-plastic paint. I even painted the inside...


All the Mustang supply places sell a kit for replacing the foam and rubber heater parts. There were a couple of extra bits in mine, so it's worth figuring out exactly where you're going to stick each piece before you start gluing up the foam.


Speaking of glue, I used the 3M "Yellow Weatherstrip & Gasket adhesive." (Part #3M8001 if you order from NPD).


You want to apply the adhesive to both surfaces, and it helps if you've got a spreader. I had to improvise with a bit of folded over card board from the packet the glue came in. It wasn't ideal.


Wait five minutes or so, and then slap the two surfaces together. The opportunity for repositioning/lining up is minimal once the two surfaces are in contact.


I used a bunch of different sized pop rivets to get it all back together.


When it came to the heater core I was tempted to put the old one back...but ultimately I decided to replace it. I also bought a pair or reproduction end caps, which were missing from my unit.


All back together....and back into the box. I'm more than three years into the project now and the pile of boxes of parts finally includes more stuff that is finished than still "to-do!"


The driver side ventilation duct was in similar shape to the heater unit (and it was packed in the same box), so I took care of that at the same time.


The seal for the duct does not come with the heater kit, so you need to buy that separately. It goes on the same way though, and I used a few bulldog clips to hold it in place while the adhesive cured.


Onto the heater motor. The part# clearly starts with C5 (65), so it's reasonable to assume that it's original.


It looked in poor enough shape to to be original too....plus I accidentally chopped the terminals off when I removed the motor from the car. Oops.


After the wire wheel did it's work and the case had been re-painted, I soldered on two replacement wires and reattached the original terminals.


I also added the (almost) correct colored plastic sleeves which I got front my new heat-shirk tubing kit. The bolts which hold the two halves of the motor case together were zinc plated long ago.


Finally I sourced a replacement plastic plenum chamber from NPD. There wasn't strictly anything wrong with the original cardboard one.....but I decided a while back that I'm not going to put anything back which smells like "old car," so the original cardboard chamber had to go.


The ducting for the defrost vents went the same way....

Tuesday, March 5, 2013

351 Windsor: The Tear Down

So where was I? Well, I had a day off from real life in mid November to start tearing down the 351W. This project actually began on my birthday in 2009 when my friend James came by to show me how to put the car or jack stands. Since then it has become traditional for me to work on the car on my birthday. One year I spent the best part of the day driving out to Mustangs Plus in Stockton so I could pick up my new leaf springs. The problem with birthdays though, is that they only last for twenty four hours. This year all I managed to accomplish was getting the motor up on the stand and draining out the oil. Then it was back to this look for another six weeks:


My biggest worry over this period was whether I had jumped the gun by draining out the oil. I really should have waited. Oh well. When I finally did pop off the oil pan, it didn't actually look too bad. There was some white crud in the bottom of the pan. I think this comes from water getting into the oil*.


Overall the "inside bits" looked great, even close up


Now let's back up a step. One day shortly after I got the motor up on the stand my friend Brian took the time to explain to me how important it was that I marked the pistons, main caps and so on so that they would go back exactly the same way. We were having lunch at sabuy sabuy on College at the time and I ended up leaving with, like, three table clothes covered in diagrams and instructions. So, with this knowledge, the first thing I needed was some number punches. I tried really hard to get a top notch set from Granger, but I just couldn't make it happen. Fortunately HF have a once-use set for less than a price of a big mac. Probably. The only thing is....they may as well be made of plastic. In fact I think they were made out of plastic!


After a good thirty minutes of screwing around with my pseudo-plastic punches, trying to figure out how to get any kind of legible impression from them, I found that all my pistons and rods have already been marked. Or to put that another way, the engine has been apart before. Not too surprising for a forty year old motor in as good a shape as this one. So I threw the HF punches in the trash and moved on.


My new Crafstman tools made the job of pulling the pistons a piece of cake. I'm still getting used to the difference good tools make.


Next up, the harmonic balancer...and here's where it starts to get complicated. To get the balance off, you need to use a puller. I already have one of those, but before I could even worry about finding it in my tiny, overcrowded garage, I needed to get the bolt out.


First task: stop the engine from turning while I undo the huge bolt which prevents removal of the harmonic balancer. I did my usual "copy Alex" and attached some clamps to the pressure plate; I'm going to be using a manual transmission so the pressure plate is scrap at this point and I didn't worry about damaging it.


I had to carve up one of my clamps to make it fit.


I had a bunch of attempts at undoing the bolt, culminating in a two foot breaker bar fitted with the handle off the floor jack...and all I succeeded in doing was warping the pressure plate. I swung on the jack handle with my entire body weight and....nothing happened. Well nothing apart from the stand nearly fell over!


After that near-miss, I did the only thing I could do: gave up, and made arrangements to transport the motor to where a decent impact wrench could get the job done. I'm very fortunate to have several friends located nearby with the necessary tools. But first I had to get the engine into the back of the Lesboat.† Just the thought of having to re-build the "leaning tower of Pisa" I needed to get the motor onto the stand was enough for me to enlist the help of my neighbor this time. I prepared a special dolly to use as a transport cradle.


Took off the main caps just to make it a all a little bit lighter.


And then I had an idea: The only thing still holding the crank in place was the timing chain! After this realization I couldn't destroy the chain fast enough: I used a flat blade screw driver to destroy it one link at a time‡. I would of broken out the screaming cutting wheel of death, but fortunately I lent that out to a buddy, otherwise who knows how much damage I might have done...


Had to wiggle it a bit, but the crank came out WITH the harmonic balancer still attached. Nobody I've talked to has ever seen/heard of somebody doing this before. I think my novice status means I often take the unorthodox route without any concern.


Pulled out the old cam and the lifters...


Tossed everything into the Lesboat and set sail for Stirtz Machine in Oakland.


The guys at Stirtz Machine have been building motors since the dawn of time. On the days when the shop is closed they build some of the finest race cars ever seen in the Bay Area. They also did me the favor of hitting my troublesome harmonic balancer bolt with the biggest impact wrench in the shop....and after multiple attempts the bolt gave it up. I left the block for magnuflux and sonic testing which is an incredibly cheap $40. Hopefully it will pass....

Have you spotted it yet?

Back in the garage, the engine dolly looked very empty. I felt like a well loved guest had departed; someone that would be gone for a while. I tried to take my mind off the feeling of emptiness by pulling the balancer off the crankshaft and freeing up the timing chain cover. But the only thing that could cheer me up was a good 30 minutes looking through the Summit Catalog :))) 


(*One day I might write up the story of why I know this).
(† Another one for the future).
(‡ Intended).